BENEFITS,
COSTS AND OPERATING EXPERIENCE
AT TEN AGRICULTURAL ANAEROBIC DIGESTERS
ABSTRACT
Farmer motivation for building
and operating anaerobic digesters has expanded from solely energy benefits
to include manure treatment cost savings, nutrient conversion, odor and
pathogen control, and byproduct recovery.
Over the last 3 years, three dairy plug flow digesters (NY, CT,
OR), four covered pig manure lagoons (NC, VA, IA, MS) and three heated
mixed pig manure digester (CO, IO,IL) have been placed in operation with
AgSTAR technical assistance. The farms and their digester systems are described.
The system installation, operation and benefits are described.
A summary table by type of digester is presented to allow
comparisons of costs. Biogas recovery and use in boilers or
engine-generators is discussed for each farm.
Start up and operational lessons learned are presented. The USEPA,
USDA and USDOE sponsor the AgSTAR Program to encourage farm methane
recovery from anaerobic digestion.
Introduction
Anaerobic digestion is more
extensively used outside of the US where treatment of animal waste has
been a concern for a longer
time. An anaerobic digester
is a vessel designed to retain decomposing manure for sufficient time at
the designed operating temperature to allow the growth of methanogenic
bacteria in a “steady-state”. Electricity
and heat production are direct benefits of anaerobic digestion. The
effluent of a digester has an earthy smell with some ammonia present. The
first dairy digester systems in the US were installed principally to
produce energy during the energy crisis.
The first pig manure digester systems in the US were installed
principally to control manure odors. Today, farmer motivation for building
and operating anaerobic digesters has expanded from direct energy benefits
to include key non-energy benefits such as: odor control, improved manure
handling, mineralization of organic nitrogen, weed seed destruction,
pathogen reduction and byproduct production such as digested dairy solids.
Complete Mix Digesters
Complete mix digesters are used
to treat waste with 3 to 10% total solids and adequate volatile solids to
produce enough biogas (60% methane, 40% carbon dioxide) to maintain
digester temperature. Three
complete mix digesters were built on farms with pull plug manure
collection in cold climates. All are heated with biogas-heated water and
mixed to maintain a high level of bacterial activity. All units represent
a cost savings over using an ambient temperature lagoon designed to
Natural Resources Conservation Service (NRCS) or American Society of
Agricultural Engineers (ASAE) standards to perform the same level of
treatment for odor control. Ambient
temperature lagoons would be 10-20 times larger than these digesters to
perform the same function. The
design and operation goal of the Apex Digester is consistent biological
stabilization of waste and odor control, while the goal of Colorado Pork
and Swine USA is optimization of biogas production and use while
stabilizing the waste.
Apex Pork - 8,600 Head Pig Finishing Facility,
Rio, IL
Apex Pork has 8,600 hogs in 9
buildings with pull plug manure collection.
Three years of seasonal odor episodes from the manure storage pond
were not acceptable to downwind neighbors. The farm chose Resource
Conservation Management, Inc. to design an innovative, low cost, heated,
mixed covered earthen lagoon digester.
A bank-buried insulated floating cover is installed on the 36.3 x
48.5 x 5 meter (120 x 160 x 16.5 ft) lagoon which can hold roughly 20 days
worth of manure. The digester produces enough methane to fuel a boiler to
heat the digester and flares unused methane.
Stabilized digester effluent flows to the storage pond.
The pond no longer emits odorous gases. The primary benefits to the
owners are odor reduction of stored and field applied manure. There have
been no odor complaints since the digester was installed. Compliance
investigations by state regulators stopped. The digester is able to
accommodate the variation in manure loading rate that results from
all-in-all-out operation.
The digester started up in
about 30 days switching to biogas from propane in June 1998. By mid
summer, 1998 the system was producing 1,020 m3
(36,000 ft3) of biogas per day. The unit was running well when a
microburst damaged the gas collection cover and nearby buildings in August
1998. The partial cover was
replaced with a bank attached floating cover over the whole lagoon in
October 1998. Concurrently
the farm was emptied of pigs to allow building renovations and a change of
pig production technique. The
farm, originally a continuous flow facility, converted to all-in-all-out
operations. Digester heating began in December 28, 1998.
The boiler system was switched to biogas January 24, 1999 and has
run full time with little or no maintenance since. The digester gained
temperature during the coldest times of the year. The digester has been
through 3 grow-out cycles without problems.
The system is simple to operate and the owner only spends about 10
minutes daily to check the system.
Several lessons of this project were: 1. A bank-buried complete
lagoon cover, though a more expensive first cost, is less expensive to
maintain than a floating edge partial cover.
2. Inexpensive cover materials such as 20 mil HDPE coated fabric
can present problems in extreme weather.
3. Pig operations can
change rapidly and radically and present a completely different waste
stream.
Colorado Pork, Lamar, Colorado and SWUSA,
Thayer, IA -
5,000-sows farrow-to-wean each
The farms are very similar in
size and operation. Colorado
Pork has about 600 more pigs growing as replacement gilts. However, the
farm buildings and equipment are different.
Both facilities were built in 1997-8 on sites that had been range
or pasture. Environmental concerns of neighbors and state authorities
prompted both owners to weigh waste management alternatives.
Both chose complete mix digesters with separate storage to: 1.
biologically stabilize manure, eliminate odor and optimize methane
recovery for electricity production. 2. reduce their investment in waste
management and 3. avoid problems with regulators by installing an
environmentally beneficial system.
Periodically, plugs are drained
to a concrete collection tank and then pumped to the 2,100-2,200 m3
concrete tank digesters. The digesters are heated, mixed and covered by
two biogas inflated plastic gas collection domes. Effluent at Colorado
Pork flows into a nearby basin to be evaporated, while SWUSA effluent is
stored in 2 concrete tanks for annual application to cropland.
Biogas fuels Caterpillar 3306 engines attached to 80 kW generators.
All electricity produced is used on the farms. Heat, recovered as
hot water from the engine and exhaust, is used to maintain the appropriate
temperature in the digester. Biogas is automatically flared when not being
used by the engine (for example during maintenance).
The farms produce up to 60% of their own electricity needs.
The farms are not expected to have surplus electricity to sell to
the utility and do not have sales metering.
The farms chose not to sell electricity rather than submit to
uneconomical requirements and controls of the utility company. Future
plans include using excess heat in the farrowing barns.
The Colorado Pork digester
heating began August 6, 1999 using natural gas to fuel the generator.
System operations on biogas began late September 1999. The digester has
been problem-free. The engine has had typical startup mechanical problems,
however, the unit has been operating continuously. In the first 5 months,
the generator operated over 90% of the time, burning 48,160 m3 (1,700,000
ft3) of biogas and producing 140,000 kWh at and average load of 50 kW.
The system output increased to 67 kW after 2 bad sensors were found
and fixed.
The SWUSA digester was filled
and heated over a 90-day period and started biogas production in August
1999, after delays due to additional construction on the digester tank.
Full biogas yield was reached in September 1999.
The digester has been virtually trouble free.
The generator has operated 77% of the time during the first 6
months yielding 64,250 m3 (2,268,000 ft3) of biogas with an electricity
output average of 67 kW. Typical startup issues of bad sensors cropped up.
The engine was rebuilt under warranty after a breakdown due to loss
of coolant. The system had a
manure spill reach a ditch through a drain added by contractors. The local
utility and the larger transmission and distribution utility were
inconsistent on requirements for intertieing the farm to the utility grid.
Table 1 summarizes the costs and benefits of these systems.
The methane recovery system at
both Colorado Pork and SWUSA has diminished farm costs of production by
reducing the quantity of electricity purchased, while greatly improving
site odors from manure storages which were objectionable to all who
experienced them and contributing to the farm’s environmentally sound
manure management strategy. At SWUSA, the digester is annually producing about $46,600
worth of electricity at $0.09/kWh. The
annual value of electricity produced at Colorado Pork is estimated to be
$34,800 based on $0.07/kWh.
Apex paid for all labor and
material except AgSTAR assistance during cover installation, start-up and
minor troubleshooting. Total cost of all work and changes was $152,300 or
$17.75 per finisher space. Operation
and maintenance costs have been less than $1000 per year for electricity
and boiler servicing. Colorado Pork paid all project costs except AgSTAR
technical assistance. The
installed cost was $368,000 or $73.60 per sow.
SWUSA received a 100% grant for the project plus AgSTAR technical
assistance. The undifferentiated installed cost was $576,000 or $115.20
per sow. Given the similarities of the systems, the author has
no explanation for the reported $208,000 difference in system costs.
Maintenance for either system is estimated at $8,000 per year
($0.015/kWh).
|
|
Table 1. Complete Mix
Digester Costs And Benefits
|
|
|
COSTS
|
Apex
|
Colorado Pork
|
|
|
|
Earthwork, soil testing
|
$
29,000
|
$
13,900
|
b
|
|
|
Lift Station/Mix tank
|
$
0
|
$
0a
|
b
|
|
|
Digester and equipment
|
|
|
$
66,700
|
$
191,200
|
b
|
|
|
Engine-generator
|
$
0
|
$
67,000c
|
b
|
|
|
Boiler
|
$
10,900
|
$
0
|
b
|
|
|
Electrical/intertie
|
$
2,200
|
$
17,600
|
b
|
|
|
Energy building,
plumbing, elec.
|
$
11,500
|
$
35,400
|
b
|
|
|
|
Subtotal
|
$ 117,300
|
$ 325,100
|
b
|
|
|
Private Engineers
|
$
10,000
|
$
8,900
|
b
|
|
|
Engineer (AgSTAR)
|
$
15,000
|
$
30,000
|
$
30,000
|
|
|
Startup
|
$
7,000
|
$
4,000
|
B
|
|
|
|
Total Cost
|
$
152,300
|
$
368,000
|
$
576,000
|
|
|
BENEFITS
|
|
|
|
|
|
Electricity
|
0
|
$
34,800
|
$
46,600
|
|
|
Heat Energy
|
0
|
|
|
|
|
|
Total
|
0
|
$
34,800
|
$
46,600
|
|
|
|
|
|
|
|
|
a.
Included in digester
b.
Breakdown not available
c.
Reconditioned equipment
Plug Flow Digesters
Plug flow digesters are used to
treat with 11 to 13% total solids scraped manure from dairies. Plug-flow
digesters are heated, unmixed, rectangular tanks. New waste is pumped into
one end of the digester, displacing an equal portion of older material
horizontally through the digester, and pushing the oldest material out
through the opposite end of the digester.
Over the past 4 years, three 1,000 cow digesters have been built in
the US by the author’s clients. The digesters are described, benefits
enumerated and a summary table allows comparison of costs and benefits.
Craven Dairy Farm, Cloverdale, Oregon –
1,000-cow digester
Craven Farms completed a
heated, unmixed, plug flow digester sized for the daily manure production
of 1000 cows in December 1996. The winter startup was not a difficult
problem. The digester
performed without incident. The used engine generators presented many challenges and
required a lot of small repairs. However,
the used generators were $50,000 cost saving over new units.
The digester peaked when treating manure from 750 cows on site and
250 cows worth of manure from neighboring dairies.
In November 1999 the farm was sold.
The owner is expected to move in and begin operations in summer of
2000.
The digester produced about $
24,000 of electricity and $ 30,000 of digester fiber yearly.
The value of digested solids is twice the original estimates.
The digester eased manure handling and reduced the cost of
application. Pathogen
concentrations were reduced two
orders of magnitudes based on 3 sets of samples.
AA Dairy, Candor, New York - 1000 cow digester
AA Dairy Farm built and started
up a at their 550 cow facility as a boiler fired system in October 1997. The digester is sized for planned expansion.
AgSTAR provided technical assistance in all phases of the project.
Issues with New York State Electric and Gas Co. over a used
intertie panel previously approved in Pennsylvania delayed
engine-generator startup until June 1998.
Modifying the previously approved panel to conform to NYSEG wishes
cost the owner $21,000. Additional issues have arisen over NYSEG punitive insurance
requirements that are being resolved.
The digester has operated
without problems. The engine
has had occasional outages for repair.
In total the generator is operating over 90% of the time. The
system is currently producing 70 kWh, hot water and about $60/day of
digested fiber. Odor has been controlled.
The cost of manure application is substantially reduced.
Haubenschild Dairy Farm started
up a digester at their 480 cow while concurrently completing their
expansion to 1,000 cows completing startup of their generator in October
1999. The major challenge was
from the generator company who delayed equipment delivery, hence system
startup for months. The utility, Steele-Waseca Cooperative has been a
promoter of and asset to the project.
The project has been well received and promoted within the state.
The dairy has chosen to wait to install a separator to recover
solids for resale.
The digester has operated
without problems. The engine
has had occasional outages for adjustment.
The generator is operating over 95% of the time. The system is
currently producing 85 kWh and hot water to keep the milking parlor warm.
Manure handling is much easier for the owner.
Table 2 shows
the costs and benefits of these three systems.
The cost variation between the systems depends mostly on equipment
that the farms already owned and the engine-generator.
The benefits depend on the value of electricity and the value of
byproduct fiber and heat. AA Dairy funding included a $90,000 grant from
the local Soil Conservation District to improve manure management with the
balance of the cost paid by the owner.
|
|
|
|
|
|
|
|
Craven
|
AA Dairy
|
|
|
|
|
|
$
9,500a
|
$
12,500a
|
$
29,505
|
|
|
Digester
|
|
|
$
128,000
|
$
121,000
|
$
111,313
|
|
|
Engine-generator
|
$
50,000b
|
$
32,000b
|
$
119,788
|
|
|
Electrical/
|
intertie
|
|
$
12,200
|
$
33,200
|
Incl w engine
|
|
|
Energy building,
plumbing, elec.
|
$
24,100
|
$
30,500
|
$
35,245
|
|
|
|
Subtotal
|
$ 223,800
|
$ 229,200
|
$ 295,851
|
|
|
Solids Separation
|
|
$
34,000
|
$
38,000
|
0
|
|
|
Engineering (AgSTAR)
|
|
$
24,000
|
$
24,000
|
$
30,000
|
|
|
Startup
|
|
|
$
5,500
|
$
4,500
|
$
4,000
|
|
|
|
|
|
$
287,300
|
$ 295,700
|
$
329,851
|
|
|
BENEFITS
|
|
|
|
|
|
|
Electricity
|
|
$
24,000
|
$
30,000
|
$
38,400
|
|
|
Digested fiber
|
|
$
30,000
|
$
21,900
|
0
|
|
|
Heat energy
|
|
$
0
|
$
3,500
|
$
5,000
|
|
|
|
Total
|
$
54,000
|
$
55,400
|
$
43,400
|
|
|
|
|
|
|
|
|
a.
Pump and wiring, no concrete
b.
Reconditioned, used equipment
Covered Lagoon Digesters
Covered lagoon digesters are
most successful in warmer climates south of the Mason-Dixon line.
A properly sized lagoon receives dilute either flush or pull plug
collected manure and decomposes the material resulting in year round
biogas production. Gas
production varies seasonally.
Barham Hog Farm,
Zebulon, NC - 4000 sow farrow to wean
Barham Hog Farm has 5
buildings with pit recharge. The
farm was built with a single cell treatment and storage lagoon.
The project installed a separate covered lagoon prior to the
existing lagoon. AgSTAR provided design, installation and troubleshooting
support and worked with NRCS to design the lagoon.
Lagoon construction began in July 1996.
The lagoon cover, 400,000 Btu boiler and a 120 kW generator were
installed in December 1996. Biogas
use for heating water began in January 1997.
Lagoon cover manufacturing problems limited biogas recovery and the
production of electricity, however the boiler has operated almost
continuously, providing hot water for pig mats under farrowed pigs.
The owner was refunded his money and has purchased a new 40 mil
HDPE cover. The 18 month
average for biogas recovery is 632 m3/d (22,300 ft3/d) of biogas.
Much of the year the generator is operated 12 hr/d at up to 90 kW
during the daytime and during nighttime 12
hours a boiler operated to produce hot water for Keeping baby pigs
warm . Odor is virtually non-existent. Cheng (1999) found that 30% of the
total Kjeldahl nitrogen (TKN), 75% of the P and 20% of the K was retained
in the covered cell. Cheng (1999) found pathogen reduction to be 2 to 3
orders of magnitude.
The farm has been limited to
offsetting about $18,000 per year in electricity and
about $12,000 per year in propane purchases.
The local utility is not in favor of farm cogeneration. However, odor control benefit is very important to the owner
because large subdivisions are being built within one mile of the farm.
Also, the improved biological stabilization and nutrient
mineralization in the digester resulted in the effluent from the storage
lagoon containing 60% less nutrients than before.
Consequently, the farm manure treatment and nutrient application
complies with the 1997 manure management regulations without additional
investment.
Martin Family Farm, South Boston, VA - 600 sow
farrow to feeder pig
Martin Family Farm covered the
first cell of a two cell lagoon receiving flushed manure in 1993 and began
engine-generator operations in spring 1994 with a matching grant from the
Southeast Regional Biomass Energy Program (SERBEP).
The first cover slowly sank and collected less gas each year.
In 1997, Engineered Textile Products of
Mobile, AL and Seamens Corporation contributed a demonstration XR-5
modular cover system to replace the original failed cover design.
Martin Farms installed the new cover and replaced the corroded
lagoon heat loop with radiators. Methane
recovery has been continuous throughout the project, though gas use has
not been. The farm has produced up to 397 m3/d (14,000 ft3/d) of biogas
and 600 kWh/d during the summer. Winter
gas production drops off to less than 170 m3 (6,000 ft3/d) and use has
been problematic. The farm has planned and purchased a hot water boiler for pig
mats under farrowed pigs. A
boiler will more closely match the farm labor skill and availability. Odor
is virtually non-existent, the effluent is stable and nutrient content of
the second lagoon has been reduced substantially.
The major benefit to the farm
has been odor control and elimination of objections by neighbors. The farm
has produced several thousand dollars worth of electricity.
A secondary benefit from the two cell approach has been nutrient
reduction in the second lagoon and ease of effluent management in
sprinklers on fields that are closer to the neighbors than the farm is.
Boland Farm, Williamsburg, IA - 2,700 Head Hog
Nursery
Boland Farm installed a low
cost Permalon cover in May 1998 over their manure storage basin to capture
odorous gases. The cover is a complete, bank to bank design with trench
buried edges. The basin produces combustible methane as predicted. Gas is
flared.
The cover was designed for
owner installation. The
owner, one AgSTAR support person and 6 neighbors assembled and installed
the cover over a two day period. The
owner later installed a flare with solar powered ignitor.
Combustible gas is produced and burned in August and September. The
lagoon filled for the first time in spring 1999 and was pumped out with a
pto pump that was backed down the bank and through a hatch in the cover.
Rainfall collected on the cover has been occasionally pumped off.
The cover has almost eliminated odor from the basin.
The owner states that they are now able to hang the wash outside
for the first time in years.
Cal Poly University Dairy, San Luis Obispo, CA,
400 cows
The dairy is located adjacent
to the California Polytechnic State University campus in San Luis Obispo,
California. The dairy
presently milks 180 cows with a total population of over 350 animals. Most
of the herd is housed in freestall barns.
About 90 percent of the manure is deposited on concrete and flushed
with fresh or recycled water to the lagoon. The remaining 10 percent of
the manure is deposited in the corrals and is only collected seasonally.
Solids are separated from the flushed wastewater prior to storage
in a single cell lagoon. This
lagoon has a volume of 19,000 m3 (670,000 ft3), which translates to 50 to
90 days of storage, depending upon the water used by the dairy. A new
primary lagoon was located next to the existing lagoon, and has
approximate surface dimensions of 80 x 65 m (265 x215 ft). The depth
varies from 5.2 to 3.7 m (17 to 12 ft) with 2:1 side slopes.
In May 1999, the new lagoon was completed with partial cover in
place. The gas handling system including gas blower, meter and the flare
were installed and operational. Preliminary gas measurements indicate
approximately 130 cubic meters of biogas produced daily from the partial
cover of less than 50% of the total lagoon surface area. The biogas is
being continuously flared and is maintaining a self-supporting flame. The
principle benefit to date has been reduced odor and some reduction of
nutrients in the storage lagoon water.
The university plans to cover the balance of the lagoon surface and
install a microturbine to use the biogas to produce electricity.
Table 3 summarizes the costs
and benefits of the covered lagoons.
These projects were completed with some matching funds, but not
more than 50%
|
|
Table 3. Covered Lagoon
Costs and Benefits
|
|
|
|
Boland
|
Martin
|
Barham
|
Cal Poly
|
|
|
New Manure transfer pipe
|
|
|
$
3,500
|
$6,000
|
|
|
Excavation
|
500
|
$
13,000
|
$
57,400
|
$60,000
|
|
|
Digester Cover
|
9,300
|
$
40,000
|
$
57,300
|
$54,000
|
|
|
Gas/hot water piping
|
200
|
$
|
$
4,600
|
|
|
|
Gas pump, meter, flare
|
1,000
|
$
1,800
|
$
3,200
|
$5,000
|
|
|
Engine-generator
|
0
|
$
9,200
|
$
87,540
|
$30,000
|
|
|
Hot water use equipment
|
0
|
$
0
|
$
21,600
|
0
|
|
|
Engine-generator building
|
0
|
$
7,200
|
$
8,200
|
$10,000
|
|
|
Heat loop, farm labor,
electrical
|
| |